jak w temacie, posiadam enderka 3 pro z klipperem i mainsailem, za extruder robi u mnie https://www.aliexpress.com/item/1005003 ... nav-review.
Ostatnio pojawiła się dziwna rzecz, po 1-2h drukowania extruder zaczyna stukać, silniczek momentami się cofa. Po jakimś czasie wraca to do normy, niestety ubytki w druku podczas stukania sprawiają że model się rozdziela na pół:/ Bowdena na niebieski już wymieniłem. Dodam że drukuję materiałem DD silk, temp 230-235 (próbowałem różnie) na hotendzie oraz 60 na bedzie.
Drugą sprawą jest wymiana obecnego extrudera na :
https://allegro.pl/oferta/direct-ekstru ... 3220560969
lub
https://allegro.pl/oferta/direct-ekstru ... 0928382118
Jakie są + i - takich rzeczy i czy się opłaca?
Proszę o pomoc
Mój config do klipperka:
Kod: Zaznacz cały
[include mainsail.cfg]
[virtual_sdcard]
path: /home/artur/printer_data/gcodes
on_error_gcode: CANCEL_PRINT
[mcu]
serial: /dev/serial/by-id/usb-1a86_USB_Serial-if00-port0
[printer]
kinematics: cartesian
max_velocity: 300
max_accel: 3000
max_z_velocity: 5
max_z_accel: 100
# custom
[stepper_x]
step_pin: PC2
dir_pin: PB9
enable_pin: !PC3
microsteps: 16
rotation_distance: 39.76
endstop_pin: ^PA5
position_endstop: 0
position_max: 235
homing_speed: 50
[stepper_y]
step_pin: PB8
dir_pin: PB7
enable_pin: !PC3
microsteps: 16
rotation_distance: 39.62
endstop_pin: ^PA6
position_endstop: 0
position_max: 235
homing_speed: 50
[stepper_z]
step_pin: PB6
dir_pin: !PB5
enable_pin: !PC3
microsteps: 16
rotation_distance: 7.96
endstop_pin: probe:z_virtual_endstop
# position_endstop: 0.0
position_min: -5
position_max: 250
[extruder]
max_extrude_only_distance: 100.0
step_pin: PB4
dir_pin: PB3
enable_pin: !PC3
microsteps: 16
full_steps_per_rotation: 200
# gear_ratio: 50:17
gear_ratio: 3:1
# rotation_distance: 23.44
rotation_distance: 23.132
# rotation_distance: 23.056
nozzle_diameter: 0.400
filament_diameter: 1.750
heater_pin: PA1
sensor_type: EPCOS 100K B57560G104F
sensor_pin: PC5
control: pid
# tuned for stock hardware with 200 degree Celsius target
pid_Kp: 21.527
pid_Ki: 1.063
pid_Kd: 108.982
min_temp: 0
max_temp: 250
[heater_bed]
heater_pin: PA2
sensor_type: EPCOS 100K B57560G104F
sensor_pin: PC4
control: pid
# tuned for stock hardware with 50 degree Celsius target
pid_Kp: 54.027
pid_Ki: 0.770
pid_Kd: 948.182
min_temp: 0
max_temp: 130
[fan]
pin: PA0
# Pin mappings for BL_T port
[bltouch]
# sensor_pin: PROBE_IN
# control_pin: PROBE_OUT
sensor_pin: ^PB1
control_pin: PB0
x_offset: -44
y_offset: -16
z_offset: 0.555
probe_with_touch_mode: true
stow_on_each_sample: false
[bed_mesh]
speed: 100
mesh_min: 20, 20
mesh_max: 190, 190
probe_count: 5,5
algorithm: bicubic
[safe_z_home]
home_xy_position: 117.5, 117.5
speed: 75
z_hop: 10
z_hop_speed: 5
move_to_previous: true
[display]
lcd_type: st7920
cs_pin: EXP1_7
sclk_pin: EXP1_6
sid_pin: EXP1_8
encoder_pins: ^EXP1_5, ^EXP1_3
click_pin: ^!EXP1_2
[output_pin beeper]
pin: EXP1_1
[board_pins]
aliases:
EXP1_1=PC6,EXP1_3=PB10,EXP1_5=PB14,EXP1_7=PB12,EXP1_9=<GND>,
EXP1_2=PB2,EXP1_4=PB11,EXP1_6=PB13,EXP1_8=PB15,EXP1_10=<5V>,
PROBE_IN=PB1,PROBE_OUT=PB0,FIL_RUNOUT=PC6
[display_status]
#*# <---------------------- SAVE_CONFIG ---------------------->
#*# DO NOT EDIT THIS BLOCK OR BELOW. The contents are auto-generated.
#*#
#*# [bed_mesh 30052023-test]
#*# version = 1
#*# points =
#*# -0.174125, -0.139300, -0.154225, -0.161687, -0.186562
#*# -0.027362, 0.007463, -0.017412, -0.032337, -0.052237
#*# -0.022387, 0.024875, 0.009950, 0.007463, 0.007463
#*# 0.029850, 0.077113, 0.069650, 0.072138, 0.077113
#*# -0.024875, 0.019900, 0.019900, 0.034825, 0.052238
#*# x_count = 5
#*# y_count = 5
#*# mesh_x_pps = 2
#*# mesh_y_pps = 2
#*# algo = bicubic
#*# tension = 0.2
#*# min_x = 20.0
#*# max_x = 190.0
#*# min_y = 19.990000000000002
#*# max_y = 190.0